When I sold my motor home 2 1/2 years ago, I offered to sell the buyer
my Suzuki XL-7 tow car for a nominal package price and he turned me
down. Recently, I received a call from him asking if I still had
the car, and if I would be willing to sell it to him. After some
negotiating, we agreed on a price (that was higher than originally
offered) and I sold him the car. I had delayed selling the car as
it was a true 4 wheel drive, and I have decided that living in
sometimes snowy Prescott, I wanted to keep a 4 wheel drive
vehicle. What I really wanted, now that I no longer need a
towable car, was a pickup truck, and I started keeping my eyes open for
a decent one I could afford.
After some online searching, I found a nice Nissan Frontier pickup with
a rear shell at our local Honda dealer. His offered price was
somewhat higher than some I had seen online, but in other areas.
It ticked all the boxes of
what I wanted, and as it turned out, their price was right in line
after some serious negotiating. (I hate that!) The truck
was in very good condition for its age, and I really could not afford
one much newer for a secondary vehicle which will not be driven that
much. It has a 4 liter V6 dual overhead cam engine, an automatic
transmission, and 4 wheel drive. The tires are brand new .
It is classified as a Crew Cab and has rear seats, but not much knee
room. It also has a 6 foot long bed.
The 4 wheel drive truck is in quite good condition. The LE trim
model is the one which has all the "goodies", such as power leather,
heated seats, a powered sun (moon?) roof,
premium sound system, roof
rack, super tie down system in the bed, etc. It also came with a shell over the
bed. A bottle of touch-up paint will help cure the "road rash" in
several places.
Updated radio:
With the shell on, the rear visibility from the cab is not very good,
so the first order of business was to replace the radio with one
containing a 7 inch screen and add a backup camera. I have made
this modification on my Jeep, the Tracker, the Suzuki, and now the
Frontier! My Volt came with a backup camera system, but I changed
the camera to get better resolution. Yeah! I really like backup cameras!
The original radio was a high-end unit for its day, but by today's standards is very dated. The great thing
about it is it is a double DIN size, the size most replacement radios today fit.
The radio I chose is an Atoto F7 which has several interesting
features. It supports a backup camera, a front camera, and a
spare video input. The cameras (only the backup in my case) can
be turned on independently of having the car in reverse, so you can
monitor traffic behind you as you drive. When you put the
transmission in reverse, the camera comes on, if not already on, and
backup guide lines are added. These backup lines have a feature I
have dreamed about on previous cars, but have not been able to realize
until now. The lines are fully adjustable in the setup
menu. I have mine set so the yellow side lines fairly accurately
define the width of the truck as it backs up. The green safety
cross line is 6 feet behind my bumper, and the red line is 2 feet.
Other relevant features of this radio, besides a slew of music input
options are that it supports both Android Auto and Apple Car
Play. These allow full interaction of an app on your phone
on the 7 inch screen. This is ideal for using your phone for
navigation using the car's built in larger screen.
Installation was fairly typical with the need to make a harness by
combining the pigtail harness that came with the radio with a similar
harness purchased to mate with the truck's original radio
connectors. I was able to use the original mounting brackets by
slightly slotting 2 of the mounting holes on each side. After
completing the electrical and the mechanical installation it was time
to test it. I turned it on, it lit up and showed it was receiving
a station, but THERE WAS NO SOUND!
When I discovered that I truly had the premium radio, I had to modify
my harness to include cables to plug into the various pre-amp
outputs. The plugs
to connect to the new radio are on the left, while the two white
connectors on the right plug into the truck wiring harness. The
side wires are to the backup
lights to indicate the truck is in reverse, the power cable to the camera, and the connector for the steering wheel controls.
The right picture shows that with the panels removed, there is
wonderful access to the rear of this radio. Fortunately is is
very thin, while the original
radio extended 6 1/2 inches back into the dash.
Before starting the installation, I had to determine if the truck
contained a "normal" radio or if it had the Premium Sound System.
One of the larger after-market suppliers of automotive electronics
showed for my truck a trademark label on the driver's door if it
contained the premium system. My door had no such label,
therefore I must have the normal system, right? WRONG! It
turned out that I do have the premium system, which includes an added
amplifier under the front passenger seat. Sending the amplified
audio from the radio to this amplifier would result in extremely loud,
distorted sound - if the amplifier were powered up. However, I
did not connect the "amp enable" wires when I made the harness, as I
thought I had no amp. I also discovered that the "thing" under
the rear left seat is a sub-woofer, and that I have tweeters on the
dash and in the rear doors to supplement the normal door speakers.
I rewired my harness to include wires for 4 pre-amplifier outputs using
RCA jacks on the radio in place of the speaker outputs, I also
connected the "amp enable" wire. Now it all worked just
fine. I also connected the steering wheel control wires and have
6 user definable inputs to the radio using the buttons on my steering
wheel. I chose volume up and down, rear camera on and off, and
answer and hang up the hands-free phone function.
The left shows the normal screen I like while driving with a music station playing. There are specialized screens for
every function, and the touch screen makes it easy to switch.
The right shows the backup image (in my RV garage workshop) and the adjustable guide lines. The lines do not show if you
select the camera while driving.
Cap removal and storage system:
The cap (also called a shell) on the rear of the truck is very nice and
certainly will protect any contents in the truck bed, but it also
limits the usefulness of the truck. I need a way to remove and
re-install the cap by myself, and I also need to find a place and
method of storing it when it is off the truck.
I discovered a device designed to lift items from car roofs such as
kayacks, Jeep removable tops, and pickup truck shells, and store them
by hanging them from the ceiling! It looked like a good solution,
but was over $200, and I figured I could do something similar, but for
less money. I did the rough design of several systems and did
some approximate pricing and discovered that I could not save very much
money by doing quite a lot of work! I ended up ordering the Hoister
system from Harken Inc. They make several models for different
weight ranges of loads. I chose the largest size with a weight
limit of 200 pounds. This consists of a system of marine lines
(ropes to us common folks), high quality pulleys, and a patented
anti-drop mechanism which grabs the line as you release tension on it
so the load will stay at its height, without dropping at all as you
release each pull. To lower the load, you pull the line at an
angle to the wall and the mechanism releases its grip.
Most of these systems are installed in the normal garage, however since
my garage has a very low 8 foot high ceiling, this was not an
option. Instead I decided to install it in my RV garage, now a
woodworking shop, on its 16 foot high ceiling.
I am very impressed with the overall quality of the kit. The
pulleys are stainless steel side plates with a plastic pulley
inside. If you spin the pulley, it will continue spinning for
about 10 seconds before stopping! It turns out that Harken's
primary business is producing rigging for yachts. They claim
their equipment is on all the championship yacht racers. The
quality shows.
The system has 4 drop lines coming from pulleys on a pair of 6 foot 4 inch
2x6's (I supplied them) bolted through the ceiling into the trusses. The bottoms of
these lines are connected to a pair of flat 7 foot long straps which
have a quick disconnect latch. The 4 lines are connected to an 8
to 1 ratio block and tackle which runs between the 2x6's and the wall.
The pull line drops from the ceiling at the wall and allows you to
raise or lower the 4 drop lines. With my system I can raise the
cap to about 8 feet from the floor for storage, down to about 30 inches
for placing the cap on saw horses if that should ever be desired.
Harken offers this system for either 10 or 12 foot maximum ceiling
height, but not for a 16 foot height as I have in the RV garage.
To accommodate, I had to extend each of the 4 drop lines. I
researched strong knots on-line and decided on using the Flemish bend
(also called the double figure 8 knot). This knot is proported to
be stronger than the rope, certainly stronger than the less than 50 pound load on each line.
This shows the system after the basic installation is complete. I
have yet to extend the down lines and attach the straps. I
painted the two
6 foot 4 inch 2x6's and attached all the hardware in advance. The most
difficult part of the whole job was then lifting them to the ceiling,
positioning
them correctly, and getting the first lag bolt in and tightened.
The rest was relatively easy, except for constantly climbing down,
moving the
ladder, then climbing back up. Oh, if only I had a scaffold, a bucket truck, or a scissor lift!
The 2x4 clamped at the top of the ladder was to provide me solid
support when I was working from a couple steps from the top. It
was
wonderful (necessary) to have a good hand hold when up there.
I also had to raise one fluorescent (now LED) light fixture. If
it stayed at the lower level of the others, I could not pull the line
at a sufficient
angle to release the line.lock
To solve the problem of the lines hanging down into the center of the
RV garage when the cap is on the truck, I mounted a single pulley near
the ceiling and ran a light nylon line with a caribiner
on the end. I clip this to all 4 of the lines, lay the straps
over the top and pull it all to the edge of the ceiling. A 3D
printed cleat on the wall holds it all in place.
No, this is not a circus trapeze setup! It is my way of handling
the lines when they are not in use. I fastened a small pulley to
the right of the main lifting lines and ran a light
nylon
cord which I can attach to the 4 down lines. Pulling them up to
the ceiling creates an interesting pattern, but most importantly gets
them out of the way.
One anticipated problem of running the straps around the cap is that I
have to lift the cap slightly above the edge of the truck bed so I can
pass the straps through. As the cap has a channel around the
bottom which straddles the bed wall and overlaps it by about 2 inches,
I have to lift the cap these 2 inches plus enough to actually fit the
strap under it. I made a set of 3/4 inch thick blocks to place
under the cap once it is lifted. Of course the reverse is true
upon replacing the cap. I have to set the cap on the blocks,
remove the straps, then remove the blocks and lower the cap to the
truck, again, almost 3 inches total at each corner.
The first time I removed the cap, I lifted each corner by lying on my
back in the bed and using my feet to lift the corner of the cap.
I
could then slip in the block and release the cap. This is NOT the
way to do it. I initially made a very simple tool consisting of a
vertical board and a horizontal one, pivoting on a bolt giving me about
a 4 to 1 lever ratio. I could stand this up under the corner, put
the edge of the horizontal board under the inside of the channel and
lift
it. It worked OK, but I don't like lifting by the edge of the
sheet metal forming the channel. I then re-made the tool giving
me a small pin on the end of some MDF. There are 3 locations
along each edge of the cap where the channel widens for the hold down
clips. In these areas I can get the pin up into the channel and
lift on the flat top surface. This is far better. Of course
my "quick trial" MDF pin did not last long (it did 2 corners OK, and
broke on the 3rd), but it proved the concept. Making the pin of
steel will give me a practical working tool.
The left picture shows my makeshift tool after lifting the corner and
inserting the spacer block. Taking what I learned I replaced the
outer MDF block with a piece of scrap steel,
already in a curved shape to which I welded a 3/8 steel rod. This not only
should be durable, but the extension of the pin sideways should allow
better clearance around obstructions.
I'll have to wait until I put the cap back on the truck to try it out.
I included these two photos just because I found them
interesting. The left shows what a great mirror the front shell
window makes, vividly showing a somewhat magnified view
of across the street. The right picture just caught my interest with the bright
blue sky and white clouds and showing a direct view of across the
street.
The other problem, which I did not anticipate, was during lowering the
cap back onto the truck. As the cap contacted the blocks on the
bed walls, the load on the locking mechanism reduced enough that it
locked the line, and I could not lower the cap all the way. Even
after I adjusted all the lines so that the contact was pretty well
even, the line locked before I could finish releasing all the
tension. My initial solution was to hook a short rope to one of
the down lines, and through a loop near the floor, press down with my
foot. When applying a considerable part of my body weight, I estimate about 100 pounds, the
lock released and I could pull the needed slack. This is NOT the
answer, as putting that much of my weight on a totally unstable,
hanging rope makes it hard to keep my balance.
My solution to this problem was to design and build a small addition to
the line locking mechanism which allows me to pull yet another light
line which will cause the locking pawl to be pulled away from the rope,
thus disabling the locking function. Now, after lowering the cap
to the first contact with the truck, I can pull this additional string
and easily set the cap completely down plus I can pull one of the down
lines for a little extra slack. It works like a charm.
The left shows the line locking mechanism which is a part of the fixed
end of the block and tackle. The locking pawl is seen in the lower
hole, and pressing it to the right will
release it. The right picture shows my solution. Two
aluminum plates are clamped to the locking mechanism and securely
positioned by snug fitting holes around the rivet heads.
The stainless steel rod with the loop can be pulled by the nylon line, which rotates
the bar on the right with a pin passing behind the pawl. The rotation pulls the
pawl away from
the lifting line. And yes, I did cut off the excess length of the
top rod after taking this picture. I made a slight flat surface
on the main rod so the block will not slip.
The Hoister has pretty well consumed one of the few available wall spaces remaining! In the center is the main pull
line, a safety cleat securing it, and the storage hook for the excess line. To the right is the light line which will pull
all the empty lines up high, out of the way, and below it, a small hook for storing it's excess line. The left light
line is the lock release. I could have made these a lot more compact as the safety cleat is the only one really
needing to be mounted to a stud, but I had the room and used stud mounting for everything.
In practice, this release works very well. After
lowering the cap down to contact the blocks on the truck rails, I
then pull the release line and lower just a little more to release the
stored up tension. It only takes a short,
light pull to activate the release. Then for good measure I grab one of the down
lines and give it about an inch or so extra to provide just enough slack to
easily release the latches on the straps, and provide enough slack to hook it all up next time. It is a big improvement!
Miscellaneous Mods
LED lights:
I replaced the interior dome and map
light bulbs and their dull orange glow with LED bulbs which give off a
bright daylight colored illumination. I also replaced the high
stop light and cargo light on the back of the truck cab with LED
bulbs. The old bulbs were a dark gray in color and could not have been
transmitting very much of their light through the bulb's discolored glass.
The LED's brightness and daylight color do an excellent job of
illuminating the interior. I can now read by their light, a task
I would have struggled with using the old bulbs. On the right,
the cargo lights really light up the bed in a dark garage. Unfortunately, when the
cap is on, these lights shine into a solid panel of fiberglass several
inches away. I have not yet investigated
the lighting options in
the shell, but I do know that the brake light.is duplicated above the rear window of the shell.
Hood prop bar removed:
For under $30, I bought a kit
containing 2 gas cylinders and several brackets which will hold the
hood open without using a prop bar. The installation took less
than 30 minutes and now the hood is much lighter and easier to lift the
first foot or so. From that point the cylinders are trying to
lift the hood and you need to hold it back. The hood also opens
about a foot higher than it did with the prop bar.
The two gas struts do a fine job of holding the hood open. As
shown on the right, all the brackets fit over existing fasteners, so no
holes or new fasteners are required.
Front Bumper Paint:
As received. the front bumper inset looked terrible! The black paint
was worn away and chipped, showing a gray
mottled color. I spent some time sanding and scrubbing it, and
then masked all around it. Three coats of rattle can black made
it look much better.
The only hard part about painting the bumper was the masking.
Once that was complete, the painting took about 5 minutes per coat for
3 coats. The picture above has a reflection from
the top edge of the bumper. It really is black there also.
Headlight Restoring:
When I bought the truck, the left headlight was quite
cloudy, while the right one was clear and shiny. The right was
probably replaced several years ago when the truck was involved in a
minor fender bender accident of the right front of the truck (the only one CarFax reported during its
lifetime). I used my Maguire headlight re-conditioning kit and
made both lights shine. The kit has you wet sand the lens with
1000 grit paper, then with 3000, then buff it using a polishing pad in
a drill with their polishing compound. The lens is then thoroughly
cleaned and coated with 2 coats of the Maguire preservative
compound. In addition to protecting the finish, it gives the lens
its final sparkle, which is clearer yet than after the polishing.
HomeLink garage door opener:
The truck came with a rear view mirror which is auto-dimming and
contains a display of the outdoor temperature and a compass. It
also contains a 3 channel HomeLink transmitter. HomeLink is a
system used in many automobiles which can be programmed to operate
almost all brands of garage door and gate openers. I grabbed the
instruction sheet and went through the process of programming a button
to my garage door. I could not get it to work through many tries.
The 3 left hand buttons can control up to 3 different garage door or
gate openers. The mirror is auto darkening when bright lights
hit it, and it shows the direction you are driving and the outdoor temperature.
I had read articles showing that older transmitters did not work with the latest openers.
I looked up on both the Chamberlain (maker of
my garage door opener) and the HomeLink sites. Both sites showed
that
my car should be compatible with my opener. Then I read an
article stating that if your opener has a yellow learn button and a
yellow antenna like mine, it is the latest security based system, and
will not work with older Homelinks. HomeLink makes a repeater
which accepts the signals from old transmitters and re-broadcasts them
in the form needed by the new openers. For $40 I bought one,
installed it, and all works as it should! I had not tried the RV
garage opener as the learn button was on the receiver plugged into a
ceiling receptacle 16 feet up. When I had the ladders set up for
the Hoister setup, I tried it and it worked from the start. This
receiver was installed before my truck was made, so it was natively
compatible. To avoid having to climb up in the future to program
for another vehicle, I removed the receiver from the ceiling, and
plugged it into a wall outlet down low, and ran a wire from it back up
to the opener.
The reason the car garage door opener did not work initially was that
it was replaced in 2014, and contained the latest security system.
On
the left is the repeater. The HomeLink button in the truck sends
its signal to this box, which in turn sends the new format signal to
the opener. All the previously working transmitters
including the hand held remotes and the Volt (newer) HomeLink continue to talk
directly to the opener and work as before. The truck button for
the RV garage door works directly with the opener.
On the right, the receiver for the RV garage is now about 4 feet off
the floor - no ladder needed for programming. I think I will
install a receptacle somewhat higher to give it a better
signal and to protect it. That is a coiled air hose stored above
it and if dropped could shatter the receiver. If I need a step
stool or a normal ladder to reach it there is no problem. The
problem
before was the need to bring out my 12 foot stepladder, which is a project in itself.